Here's the poop. I was playing around with getting my "Grainger" relief valve to work for boost control. I lenghtened the WG rod to keep it from over boosting. Kept shortning the valve to get the boost at a steady 17/18#. And everything seemed to be going great . (BTW, I had it set up as basic, turbo outlet-valve((ballside)) , WG). On my way home the WG rod fell off the pin due to me forgetting to put the clip on. I put the rod back on and now I only get 10# and spool is horrible. Today I put the stock set up back on and removed the valve, still only 10# and sloooow spool. I have a mild exhaust leak on the crossover pipe, but I had that prior to this debacle. Also vac gauge is reading 18/19 in/hg on it. This is driving me up a wall (slowly due to low boost ) Any help would be greatly appreciated. Thanx Guys.