Update:
Evidently earlier in the week when the FP/wiring issue surfaced.... even though the test run seemed smooth.... AFR spiked to 13.75:1 under boost..... saw about 6-8 spikes all over 13:1..... I guess the pump was cutting off... then back on.... in the end the FAST was trying to save it with 25% positive O2 correction..... anyway...
With that fixed... we went to the track.... 1st pass off the trailer.... trans brake launch 12-16 psi launch... car spun a little with a 1.61 I think 60' time... ... 6.90 or so in the 1/8..... head gasket popped at 900-1000 ft..... coasted to a 11.0....
Run was at 20 psi.... just before the gasket let go.... 02 corrections were -1.6%, -1.3%, actual AFR was 11.0:1. Early in the run.... he went straight from first to 3rd..... then realized it... and went back to second.... when things settled out in second..... the AFR and 02 corrections looked great.... within a few percent on either side of 0....
Head will come off today... get fixed... and a new gasket will be installed hopefully before the end of the week....
These cars will definately try ones patience.
I really think that run could have been well into the 10's....
Evidently earlier in the week when the FP/wiring issue surfaced.... even though the test run seemed smooth.... AFR spiked to 13.75:1 under boost..... saw about 6-8 spikes all over 13:1..... I guess the pump was cutting off... then back on.... in the end the FAST was trying to save it with 25% positive O2 correction..... anyway...
With that fixed... we went to the track.... 1st pass off the trailer.... trans brake launch 12-16 psi launch... car spun a little with a 1.61 I think 60' time... ... 6.90 or so in the 1/8..... head gasket popped at 900-1000 ft..... coasted to a 11.0....
Run was at 20 psi.... just before the gasket let go.... 02 corrections were -1.6%, -1.3%, actual AFR was 11.0:1. Early in the run.... he went straight from first to 3rd..... then realized it... and went back to second.... when things settled out in second..... the AFR and 02 corrections looked great.... within a few percent on either side of 0....
Head will come off today... get fixed... and a new gasket will be installed hopefully before the end of the week....
These cars will definately try ones patience.
I really think that run could have been well into the 10's....