At the top end of the track my drivers side front freeze plug came out, drained all the water out of the motor under my car. (Believe it or not, the car never got out of shape.)
I have no water in the oil and when driving it normally, there is not any water in the overflow but it does have a tendancy to push out a small amount and then once it's lowered its water level a bit, it doesn't do that anymore. Car doesn't run hot at all. I have a S1 block with the additional head studs. My biggest hunches are that I'm still lifting a head and doing the water push OR a leaking intake gasket. I had one stripped bolt in the head for the intake manifold but I put it together anyway (call me lazy but this was like 2 days before Nats). Could the intake gasket be the source? I do have a fair amount of blowby too but only after running it hard.
I have lockwire head gaskets and ARP studs.
When I run 30# of boost alone, it is fine. This only happens when I run the N2O which is only a 50 shot. The log files show everything is working just fine with the A/F. I also run 19º or timing with the N2O.
Any ideas?
Roger
BTW, that last run was:
1.386 - 60'
5.864 - 1/8 ET
123.15 - 1/8 mph
9.39 - 1/4 ET
123.33 - MPH
It let go well before the end of the run. Check out the 1/8 vs. 1/4 MPH. I was on a tear that pass.
I have no water in the oil and when driving it normally, there is not any water in the overflow but it does have a tendancy to push out a small amount and then once it's lowered its water level a bit, it doesn't do that anymore. Car doesn't run hot at all. I have a S1 block with the additional head studs. My biggest hunches are that I'm still lifting a head and doing the water push OR a leaking intake gasket. I had one stripped bolt in the head for the intake manifold but I put it together anyway (call me lazy but this was like 2 days before Nats). Could the intake gasket be the source? I do have a fair amount of blowby too but only after running it hard.
I have lockwire head gaskets and ARP studs.
When I run 30# of boost alone, it is fine. This only happens when I run the N2O which is only a 50 shot. The log files show everything is working just fine with the A/F. I also run 19º or timing with the N2O.
Any ideas?
Roger
BTW, that last run was:
1.386 - 60'
5.864 - 1/8 ET
123.15 - 1/8 mph
9.39 - 1/4 ET
123.33 - MPH
It let go well before the end of the run. Check out the 1/8 vs. 1/4 MPH. I was on a tear that pass.