dentmasters01
Member
- Joined
- Apr 13, 2004
- Messages
- 1,102
Ok, first the car. 109 block (thanks jack). 70 gtq, 85 lbers and a XFI sys.
Car weighs 3830 with me in it.
Two weeks prior to taking the car to Reynolds, it ran great. No problems.
I made three changes to the car before going to Reynolds. I mounted my wide band O2 on the DP from the stock location and drilled and tapped my upper plenum for the temp. sensor. Precision large front mount.
Every run the car was missing and the last run it pulled 2 deg. before half track recovered and pulled another 10 deg. at the 8 sec. mark. It netted a 6.72 at 106 and 10.55 at 122 on et streets spinning with a 1.63 60'.
I had a a/f TARGET of 11.2 and the ACTUAL a/f from the gate was 9.1 and never got above 11.1 until half track. It stayed in the low to mid 10 mostly. It was taking out 7-8 percent fuel until half track.
At half track it fluctuated from 11.1 to 11.6 but stayed around 11.3-4 most of the second half of the track. Keep in mind it's missing from the gate all the way through the traps. Egt's were in the 1200's.
This is what I don't get. I let out of it several times during the previous runs thinking its detinating but fast reads its fat and taking out fuel. Then on the last run it pulls all that timing and retards 10 deg. but goes from taking out 7 percent to adding only 2 with the targeted a/f???
I have tested the coil and wires as several people told me to do with the simulator sold by caspers. The module, coil and wires seem to be fine if I'm reading this ign. simulator right.
The front four plugs were dark and a couple were actually wet and 5 and 6 were a good clean burn. Kind of light grey. This is the main problem. Why the difference, along with the fast readings, in the plugs. Were the two that are light grey really lean under a wot situation? Ign. checks ok? Maybe injectors?
Also, my inlet temp. started out at 98 and by the end of the run the plenum air temps were at 152.6. Just put on the big precision front mount. I don't have any data from the previous front mount to compare it to, but just wondered if this is normal?
I'm at a loss because it ran so good, I made the 3 changes, the ignition sys. seems ok, but now it'seems to be missing under a hard pull.
any ideas??
Car weighs 3830 with me in it.
Two weeks prior to taking the car to Reynolds, it ran great. No problems.
I made three changes to the car before going to Reynolds. I mounted my wide band O2 on the DP from the stock location and drilled and tapped my upper plenum for the temp. sensor. Precision large front mount.
Every run the car was missing and the last run it pulled 2 deg. before half track recovered and pulled another 10 deg. at the 8 sec. mark. It netted a 6.72 at 106 and 10.55 at 122 on et streets spinning with a 1.63 60'.
I had a a/f TARGET of 11.2 and the ACTUAL a/f from the gate was 9.1 and never got above 11.1 until half track. It stayed in the low to mid 10 mostly. It was taking out 7-8 percent fuel until half track.
At half track it fluctuated from 11.1 to 11.6 but stayed around 11.3-4 most of the second half of the track. Keep in mind it's missing from the gate all the way through the traps. Egt's were in the 1200's.
This is what I don't get. I let out of it several times during the previous runs thinking its detinating but fast reads its fat and taking out fuel. Then on the last run it pulls all that timing and retards 10 deg. but goes from taking out 7 percent to adding only 2 with the targeted a/f???
I have tested the coil and wires as several people told me to do with the simulator sold by caspers. The module, coil and wires seem to be fine if I'm reading this ign. simulator right.
The front four plugs were dark and a couple were actually wet and 5 and 6 were a good clean burn. Kind of light grey. This is the main problem. Why the difference, along with the fast readings, in the plugs. Were the two that are light grey really lean under a wot situation? Ign. checks ok? Maybe injectors?
Also, my inlet temp. started out at 98 and by the end of the run the plenum air temps were at 152.6. Just put on the big precision front mount. I don't have any data from the previous front mount to compare it to, but just wondered if this is normal?
I'm at a loss because it ran so good, I made the 3 changes, the ignition sys. seems ok, but now it'seems to be missing under a hard pull.
any ideas??