what happened to these main bearings?

The first that you noticed any sort of noise from the engine was at the track after some passes?
Before taking the car to the track, no noise?

What sort of oil pan are you using? Stock? Modified?

Were you able to monitor the oil pressure throughout the passes? Including during shutdown?

What fuel were you using at the track? What ignition timing setting?

What compression ratio was the engine setup with? Was the CR accurately double checked or just assumed? Was the block deck or the head surfaced? How much was taken off?
The point I'm trying to make is, a lot of unanswered questions yet so eager to throw the machinist under the bus. Did I miss something?
 
Lack of lube. Or in simpler wording the engine ran without oil pressure at some point. Could have been on initial startup or for a couple seconds under power. Fwiw the rods typically wont show the same wear as the mains since they require a lot less oil.
 
Could it be that

Your oil filter is the problem? Been following this thread and to my suprise no one has mentioned oil filter. Either one without anti-drain back provisions or not functioning giving you dry startups. I was involved with an engine that the mains were identical to these--rods were not near as bad (caught it early). These bearings have definately been run a short period without oil pressure.
 
My vote goes to the previous detonation damage knocking the main bore out of round, as Chuck said. Machine the caps and align hone or bore/hone the block - it is very, very difficult to "check" if a block needs at least an align hone without just going ahead and honing it and seeing how much material comes off and where. Plus, with the fretting on those caps they won't seat as tightly in the registers and will be more prone to keep moving around, until you machine off all that damage. You might think about going ahead and stepping up to two center billet caps since you already need all the machining anyway, so the cost difference would just be the caps.
 
it looks like the crank can go .010 so i think that i can rebuild this motor. i'll probably do billet caps on the front 3. what's another $75 for the front main at this point.
 
could there have been a problem with the relief valve in the oil pump? maybe being stuck closed or open? i took the pump apart and it looked ok and everything seemed to move freely. i'm just trying to come up with some additional things to double check.
 
ok, last post until i get the parts to a machine shop. i was in the garage last night and noticed that the front galley plugs are threaded, and the passenger plug is sunk into the block a little. i shined a light through the #1 main passage and i could see a few threads of the plug in the oil passage. it wasn't completely blocked but i probably shouldn't be able to see any of that plug in the oil passage right? could that be enough to restrict the oil flow to the mains? i'm not real clear on how the oil travels through this engine.

everything on the oil pump checked out. i blueprinted it using the instructions on vortexbuick.

i'm hoping to get it back to the machine shop after labor day.
 
Many yrs ago..

ok, last post until i get the parts to a machine shop. i was in the garage last night and noticed that the front galley plugs are threaded, and the passenger plug is sunk into the block a little. i shined a light through the #1 main passage and i could see a few threads of the plug in the oil passage. it wasn't completely blocked but i probably shouldn't be able to see any of that plug in the oil passage right? could that be enough to restrict the oil flow to the mains? i'm not real clear on how the oil travels through this engine.

everything on the oil pump checked out. i blueprinted it using the instructions on vortexbuick.

i'm hoping to get it back to the machine shop after labor day.

Jim Ruggles did my 109. The screw in plugs were a pet peeve of his. He said many do the mod, but don't machine the plugs to prevent blockage. The plugs he used were THIN!
He also described problems w/ the line hone process. Due to the short length of the block, the line hone bar can "flop around", and make the end bores bigger than the centers... He claimed that Sunnen had a trik to prevent this. Never did say what it was....:D
 
also

Jim Ruggles did my 109. The screw in plugs were a pet peeve of his. He said many do the mod, but don't machine the plugs to prevent blockage. The plugs he used were THIN!
He also described problems w/ the line hone process. Due to the short length of the block, the line hone bar can "flop around", and make the end bores bigger than the centers... He claimed that Sunnen had a trik to prevent this. Never did say what it was....:D

He also said to do a line bore right--need to torque heads with gasket on.
 
machine shops

Some people like to think of machine shops as doctors (know everything and never make a mistake) Just remember " someone has to finish LAST in the class". I've had the machinest and the Dr.
 
I had bearings like that once!

was because I didnt wash out the oil galleys after machining the crank before assembling. crank was full of shavings.

A.j.
 
Yep..

Some people like to think of machine shops as doctors (know everything and never make a mistake) Just remember " someone has to finish LAST in the class". I've had the machinest and the Dr.

I've been on both sides of the fence...
B4 I became a mechanic, I was a brain surgeon..:eek::D:D

The ONLY problem I have w/ this particular shop is, they decided it was a problem based on what they were told during a fone call...
look how many "opinions" that have been offered here, and we can at least see some pictures.
 
Some people like to think of machine shops as doctors (know everything and never make a mistake) Just remember " someone has to finish LAST in the class". I've had the machinest and the Dr.

Made me laugh on that one Leo :biggrin:
 
I've seen this type of problem when using high volume oil pumps and stock pans. The pan was pumped dry causing no oil pressure. Not trying to say this happened, just something I've seen in the past.
 
I think that the HV pump did contribute to this problem. Mainly the cold start pressure being too high. My shop mentioned that when oil pressure is too high it can actually push the crank down into the main bearings in the cap.

I talked to the local GN expert, JaysGN, and he strongly advised against the high volume pump. A lot of people talk bad about the oiling systems in these cars but there are a lot of stock shortblock turbo 3.8's running around with well over 100K miles. The oil system only seems to be a problem when people start messing with it. I will for sure be setting my clearances around .002 (again) and running a stock oil pump.

Other than that, my block, pistons, and 5 rods look OK. I should only need to cut the crank .010, size a rod, and bore the line with some billet caps to be back in business. I sent the turbo back to Limit just to check it. It only has 800 miles on it but a lot of material could have gone through it. I'm also going to eliminate the stock oil cooler.
 
[QUOTE=ryan319;2585836. My shop mentioned that when oil pressure is too high it can actually push the crank down into the main bearings in the cap. I can buy this cause my main bearings in the cap where a lot worse than the ones in the block.

Another case of the shop telling you anything. Think about it. Why would the bearings in the block ever show wear? ALL the load is on the cap bearing--always trying to push the crank out the bottom.
 
ryan319;2585836. My shop mentioned that when oil pressure is too high it can actually push the crank down into the main bearings in the cap. I can buy this cause my main bearings in the cap where a lot worse than the ones in the block. Another case of the shop telling you anything. Think about it. Why would the bearings in the block ever show wear? ALL the load is on the cap bearing--always trying to push the crank out the bottom.[/QUOTE said:
I'm not saying the HV pump caused the problem, but i think that it was a problem, or one of a few. I've known one of the guys at this shop for a long time and i don't think that he would bs me. which is why i never publically bashed the shop or put their name on the thread for others to do so. i just want to know why it failed so i can fix it right.
 
Detonation

That is what made the ends of the main bearing move inward and the cap walk. It was all over after that.

Same thing happened to the rod bearing in the third picture.
 
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