Daniel Jost
Squirtin six
- Joined
- Oct 11, 2003
- Messages
- 1,288
Well after having my car apart for over a year changing the following; Headers, alternator swap, charge pipes, alky, flex fuel sensor, custom harness, vacuum brake swap, and mounting CNP coils on valve covers I finally got it back together... Only to find a plethora of unrelated problems. I first had a converter noise that was the stator making a whining noise, after replacing it the trans was spewing fluid which was coming from a cracked TV cable grommet, then I broke a rocker arm, then a valve cover had a crack and was leaking... After I thought I got everything fixed I take it out for a ride and after about 50 miles the car would make boost very slow and would only make maybe 15PSI (ECM set at 24#), before I could make it home the car no longer would make any boost! After pulling off the wastegate I noticed that the lever would go past closed... I pulled the pipe off and found there was no puck on the shaft, and it was nowhere to be found in the exhaust system either. All this has happened within 200 miles on the car since I got it back out, am I just a very unlucky person or has anyone else had this happen with the RJC "Large Puck"? The puck was part of the flange and puck setup I bought about 4 years ago from RJC when I built a custom DP, and it has been great until now.
,Dan
,Dan