t3intercooled
Member
- Joined
- Jul 20, 2004
- Messages
- 844
Just as the title says. I am in dire need of help. My scanmaster readings are not normal. Here is essentially what has occured up to this point. I am at a complete loss as to what to fix or where to look.
Car drove very well starting out this year. Then do to unforseen medical expenses I had to sell everything I could to cover monthly bills that were required (Gas, Electric, etc). Parts that I had on and sold are as follows:
Turbo Tweak chip and 80lb injector combo to be able to work with a UNMODIFIED stock computer.
Accufab 70mm throttle body and plenum with RJC power plate
Precision full ball bearing turbo
Angled IAC boss
Computer modded for injectors
Then I had my daily driver take a shit so I was forced to buy what I could to get the GN running. I wasn't looking for speed just reliability. Parts that I purchased to get it running are as follows:
Stock rebuilt Turbo
38lb injectors and turbo tweak 93 octane chip from jdpolzin
Mass air flow sensor
Stock Computer
Stock throttle body, plenum, & RJC powerplate
Brand New Walbro 340 from Full Throttle
Once I recieved those items I put everything in and the car ran good for 2 or 3 months. No detonation gauges read great. Just a blip of knock when it would shift but thats it. Then literally one day was idleing ok but then detonation occured when I was at a stop and began pressing the throttle the O2 readings would drop lean at first then if I eased it up to speed the O2 readings would be up at the 7-800s. That occured for a while but that was still my ownly vehicle. As long as I slowly eased up to the speed I would have the detonation.
I didn't change a single thing and while ideling in park, drive, reverse, etc. I noticed my O2 readings were 045, 075, etc. I know that the O2 readings are telling me its lean. As I said the chip, injectors, brand new full throttle walbro worked great for a while then literally the next day it started showing the lean readings. Now I haven't driven it since it began going wonky, so everything listed here is while it was parked running not driving so it wouldnt hurt the motor if it was lean. I began scrolling through the scanmaster and the volts were reading 12s and eventually dropped to 8s, so I figure being the pump is hotwired thats the reason for the leaan condition. Put a brand new alternator and to be safe a battery in and still same scanmaster readings.
I included videos of scanmaster reading, fuel preesure, and oil pressure. Im open to testing, checking, or replacing anything I need to. Being we have VERY knowledgable people on this board I figured this is the best place to start. Thank you to everyone who assists, it is GREATLY appreciated!
Car drove very well starting out this year. Then do to unforseen medical expenses I had to sell everything I could to cover monthly bills that were required (Gas, Electric, etc). Parts that I had on and sold are as follows:
Turbo Tweak chip and 80lb injector combo to be able to work with a UNMODIFIED stock computer.
Accufab 70mm throttle body and plenum with RJC power plate
Precision full ball bearing turbo
Angled IAC boss
Computer modded for injectors
Then I had my daily driver take a shit so I was forced to buy what I could to get the GN running. I wasn't looking for speed just reliability. Parts that I purchased to get it running are as follows:
Stock rebuilt Turbo
38lb injectors and turbo tweak 93 octane chip from jdpolzin
Mass air flow sensor
Stock Computer
Stock throttle body, plenum, & RJC powerplate
Brand New Walbro 340 from Full Throttle
Once I recieved those items I put everything in and the car ran good for 2 or 3 months. No detonation gauges read great. Just a blip of knock when it would shift but thats it. Then literally one day was idleing ok but then detonation occured when I was at a stop and began pressing the throttle the O2 readings would drop lean at first then if I eased it up to speed the O2 readings would be up at the 7-800s. That occured for a while but that was still my ownly vehicle. As long as I slowly eased up to the speed I would have the detonation.
I didn't change a single thing and while ideling in park, drive, reverse, etc. I noticed my O2 readings were 045, 075, etc. I know that the O2 readings are telling me its lean. As I said the chip, injectors, brand new full throttle walbro worked great for a while then literally the next day it started showing the lean readings. Now I haven't driven it since it began going wonky, so everything listed here is while it was parked running not driving so it wouldnt hurt the motor if it was lean. I began scrolling through the scanmaster and the volts were reading 12s and eventually dropped to 8s, so I figure being the pump is hotwired thats the reason for the leaan condition. Put a brand new alternator and to be safe a battery in and still same scanmaster readings.
I included videos of scanmaster reading, fuel preesure, and oil pressure. Im open to testing, checking, or replacing anything I need to. Being we have VERY knowledgable people on this board I figured this is the best place to start. Thank you to everyone who assists, it is GREATLY appreciated!