I went to the track for the second time since I got the car tonight. Here is a thread that kind of sumarizes the first time to the track. http://www.turbobuick.com/forums/showthread.php?t=154170
My best run was a 1.933 60 ft, 8.6 @79.48 in the 1/8, and 13.579 @ 97.93 in the quarter. Anyway, my mph didnt really change much, but I have installed the stall converter since then, and think that is what made most of the difference in time. I have also installed new valve springs, and series 2 coil pack and coils(the ignition module went bad days after my last trip to the track) since I had it to the track last. I was hoping that one of those would be the reason why it seems to fall of some up high.
The one problem I know I have, is that the one of the flanges on my crossover pipe is messed up a little, and wont seal properly. I plan to fix that in the near future. Could that cause the the car to lack that much in mph? I am running around 15-16 lbs of boost. I didnt have a scan tool with me, so I turned down the boost a couple pounds to make sure it wasnt getting kr and slowing it down up high, and my times got slower, and I lost a couple mph, so I turned it back up.
Mods are in sig. cant figure out what is causing the problem. I think that the exhaust leak might be contributing to it though.
Ben
My best run was a 1.933 60 ft, 8.6 @79.48 in the 1/8, and 13.579 @ 97.93 in the quarter. Anyway, my mph didnt really change much, but I have installed the stall converter since then, and think that is what made most of the difference in time. I have also installed new valve springs, and series 2 coil pack and coils(the ignition module went bad days after my last trip to the track) since I had it to the track last. I was hoping that one of those would be the reason why it seems to fall of some up high.
The one problem I know I have, is that the one of the flanges on my crossover pipe is messed up a little, and wont seal properly. I plan to fix that in the near future. Could that cause the the car to lack that much in mph? I am running around 15-16 lbs of boost. I didnt have a scan tool with me, so I turned down the boost a couple pounds to make sure it wasnt getting kr and slowing it down up high, and my times got slower, and I lost a couple mph, so I turned it back up.
Mods are in sig. cant figure out what is causing the problem. I think that the exhaust leak might be contributing to it though.
Ben