I've been following 87chriss's post and I have exactly the same problem. Here are my scanmaster numbers after a 25 minute "easy" drive after resetting ecm:
AF-04
L8-29
Bat-13.7
INT - jumps 137-142
BL - 142 (light cruising blm is 138)
CLT - 164
ATS - 60
R-925
TPS-.42
IAC-00
I just finished having the driver's side header welded around the outside of the flange. Also had it surface planed. I am using felpro gaskets...I have read all the feedback suggesting not to use gaskets, so thinking about it. The noticeable "tick" is now gone after fixing the header.
I smoke tested it and used the hose trick and also used seafoam and can't find any other exhaust or vacuum leaks. I have 18 in. of vacuum in park at idle.
I pulled plugs and they are definitely showing lean conditions.
Fuel pressure is good at both key on/line off, and at running idle.
I am running about 100 octane which is left over from my mix when I was trying to tune. My chip is burned for 91. Could this be the problem?
AF-04
L8-29
Bat-13.7
INT - jumps 137-142
BL - 142 (light cruising blm is 138)
CLT - 164
ATS - 60
R-925
TPS-.42
IAC-00
I just finished having the driver's side header welded around the outside of the flange. Also had it surface planed. I am using felpro gaskets...I have read all the feedback suggesting not to use gaskets, so thinking about it. The noticeable "tick" is now gone after fixing the header.
I smoke tested it and used the hose trick and also used seafoam and can't find any other exhaust or vacuum leaks. I have 18 in. of vacuum in park at idle.
I pulled plugs and they are definitely showing lean conditions.
Fuel pressure is good at both key on/line off, and at running idle.
I am running about 100 octane which is left over from my mix when I was trying to tune. My chip is burned for 91. Could this be the problem?