I was out dusting off the GN for the 2nd time. First time out no problems,20lbs boost no knock, no problem. I still hat to change out anti-freeze to rmi-25. Drove it about 1mi to where I was going. It sat for about an hour. About 1/2 way home leaned on it to check for knock from a 45mph roll,--BOOM,Bang or just a very bad sound. It started missing bad,I was able to feather the pedal long enough to get it to a church parking lot engine light on. It had died about 5seconds after making the turn in. I got out popped the hood, and the stock intake tube was blown off the throttle body and the plug in the small hole that used to go to filler tube was missing.
I was barely able to push the intake back on TB, so that was tight before it came off. It fired right up,no light. Drove1/3 mi home,parked it. Might have heard a VERY slight ticking from joint at up-pipe.
Today I went out to check things out. Dead battery,which I never really checked because it fired right up. BUT..
I disconnected intake tube to check it out. I heard some thing inside ratteling. Pulled filter and the front screen from MAF was almost bent in half,broken retainer clips also.
The battery is on charger,IAT sensor re-sealed and new plug sealed in place.
Will hook up TL wed and see if it tells me anything. No oil floating in rad, no water on dipstick, plug wires on ect.
NOW WTF happened?? I never heard of this one. Like I said ran smooth on the drive home.
I was barely able to push the intake back on TB, so that was tight before it came off. It fired right up,no light. Drove1/3 mi home,parked it. Might have heard a VERY slight ticking from joint at up-pipe.
Today I went out to check things out. Dead battery,which I never really checked because it fired right up. BUT..
I disconnected intake tube to check it out. I heard some thing inside ratteling. Pulled filter and the front screen from MAF was almost bent in half,broken retainer clips also.
The battery is on charger,IAT sensor re-sealed and new plug sealed in place.
Will hook up TL wed and see if it tells me anything. No oil floating in rad, no water on dipstick, plug wires on ect.
NOW WTF happened?? I never heard of this one. Like I said ran smooth on the drive home.