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SignUp Now!I got the IAC perfect and that changed nothing, so i was talking to brian at gbody parts and he was saying it sounded like to much fuel. So i go to adjust my FP witht he regulator and with the line off it was showing like 50 something. So i start screwing and it doesnt seem to want to move but finally does after alot of screwing, but it wont ever go below the 40psi mark. And when i reconnect the line the gauge doesnt change at all. What do you guys think is going on with that?
I got the IAC perfect and that changed nothing, so i was talking to brian at gbody parts and he was saying it sounded like to much fuel. So i go to adjust my FP witht he regulator and with the line off it was showing like 50 something. So i start screwing and it doesnt seem to want to move but finally does after alot of screwing, but it wont ever go below the 40psi mark. And when i reconnect the line the gauge doesnt change at all. What do you guys think is going on with that?
Ok im going to try and get that FP thing sorted out first like you said, to get the PSI to drop any i had to screw it alot. I felt like the screw was about maxed out when it finally went down to 40psi. And it deffinatly did not drop any psi when i hooked the vaccum line back up. And yes i had the car running and warmed up before i did this. I used to be able to spool the car just fine and my tranny went out. So i had it rebuilt and waited about a year to put it back in. When i did i was with this problem. Is it possible the FPR went bad from sitting? I also have another gauge and the stock FPR to try out next time so i should be able to pinpoint which is the problem.
bad converter ? lock up clutch come apart or what exactly what failed just wondering I had a converter go bad but it was were the input shaft slides threw the converter don't know if it hurt the transmission.that's why I was wondering when you said took out new transmission metal or clutch material go threw the pump ?Sorry to bring this back from the dead but wanted to clear it up incase it might help somebody else one day. The problem was the torque converter was bad, ended up taking out that new transmission...
So very true....Yup, these kinds of threads are way more helpful when the cause of the problem is made known once found![]()