First off, hi all I'm new to the board and this is my first post. Quick history on my trans I got used with unk mods but would bang 2nd, and hit 3 and 4 real hard too. About 20,000 miles later and about 100+ high 12 low 13 passes later just driving on the street I lost OD and it started whining like a power steering pump with no fluid. It had a rebuilt restalled D5 when I installed it. I drove home in drive about 5 miles parked car overnight tried it the next day and same problem. Removed trans, rebuilt with Alto red clutches and kevlar band and 13 vane pump with a friends help who is a certified GM tech fo 15 years.
I'm not sure but while apart it seemed to have a B&M shift kit with the spacers no spings on acumulators and 3 holes drilled bigger than stock in the X plate. It also had 2 balls removed. Stock gov. and servo.
I reinstalled it with a used Vigilante I had about 3400 stall. No changes made internally except enlarging the pump drainback hole. The trans now shifts so so 1-2 and I have to lift off the throttle alot to let it go to 3 or it just slips and 3-4 feels worse than stock. My car is an 84 regal with sorta stock 87 GN motor trans and rear. Any Ideas what went wrong. Sorry for the long post.
I'm not sure but while apart it seemed to have a B&M shift kit with the spacers no spings on acumulators and 3 holes drilled bigger than stock in the X plate. It also had 2 balls removed. Stock gov. and servo.
I reinstalled it with a used Vigilante I had about 3400 stall. No changes made internally except enlarging the pump drainback hole. The trans now shifts so so 1-2 and I have to lift off the throttle alot to let it go to 3 or it just slips and 3-4 feels worse than stock. My car is an 84 regal with sorta stock 87 GN motor trans and rear. Any Ideas what went wrong. Sorry for the long post.