In order to get the TSM car ready for the Morocco event, I took FAST V6 down to the dyno at Competition Motorsports in Cincinnati with Lonnie Diers for some "real tuning." The engine setup was the same that I had been running for years with the exception of aluminum heads, 72pph injectors (up from 52s) and Cometic head gaskets. Mind you I have been beating on this stock block with stock internals for almost 10 years now.
First pull netted just under 500HP with 23psi boost and a quite-lean air:fuel ratio (like a maximum of 13.5:1) burning straight C-16.
On the Second pull I added another 4% fuel (which I found out later added 15HP) but at ~5,700 the engine stumbled, made a Bang! and died...then bolts started falling out of the engine compartment...and then a much-larger-than-usual oil leak started dripping.
The ensuing conversation went something like this:
"What happened?"
"I think I just blew an engine"
"Sounded like a timing chain let go"
"Where's all that oil coming from?"
"Where them bolts coming from" ... you get the idea?!
I hit the starter and with a valve cover breather off, we could see the valve train wasn't moving. As such, we figured it was the chain. Upon dissasembly, things took a turn for the worse.
I am of the opinion that the RJC Engine Girdle contained the mess as much as possible. It could have been worse. See the details
<<HERE>>
First pull netted just under 500HP with 23psi boost and a quite-lean air:fuel ratio (like a maximum of 13.5:1) burning straight C-16.
On the Second pull I added another 4% fuel (which I found out later added 15HP) but at ~5,700 the engine stumbled, made a Bang! and died...then bolts started falling out of the engine compartment...and then a much-larger-than-usual oil leak started dripping.
The ensuing conversation went something like this:
"What happened?"
"I think I just blew an engine"
"Sounded like a timing chain let go"
"Where's all that oil coming from?"
"Where them bolts coming from" ... you get the idea?!
I hit the starter and with a valve cover breather off, we could see the valve train wasn't moving. As such, we figured it was the chain. Upon dissasembly, things took a turn for the worse.
I am of the opinion that the RJC Engine Girdle contained the mess as much as possible. It could have been worse. See the details
<<HERE>>