When did this start?[/quot ] this started about the time i went to the 6765 dbb billtet turbo last year. Pushed head gasket early spring this year were rjcs with studs. I changed to aluminum heads and cometics at this time about 6 weeks ago.
started before cometics went so i thought waste gate actuator so replaced it,with new turbo smart actuator that has a 14 psi spring in it,and same rod length etc as orginal.
You have a rubber hose that is connected to a port on the compressor housing on one end and the boost solenoid or controller on the other end. You also have another hose that goes from the boost solenoid or controller to the wastegate actuator. If either or both of these hoses is cracked,broken,or disconnected at either end,the boost pressure will not be allowed to open the wastegate because it will leak into the atmosphere. If the wastegate doesn't open the turbo will over boost.
i dont have any controler in car or solenoid,solenoid it is turned off in chip.so it is disconnected. line goes from turbo to actuator thats it. i have at idle 18 in hgs of vaccum according to gauge,wideband o2 is reading 14.1 in park at idle. car runs flawless except for boost issue. i replace line from actuator to gate with new same issue. puck in rjc down pipe is 1 5/8 came with pipe and flange new last year.