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Building a 7sec 87GN Drag-n-Drive car with V6 Stage 1 heads!

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Well Sick Week didn't go as planned.

We got there Saturday to test and had a wonderful day. The track was on point, the weather was perfect, the car was running well and we ended the day with a 1.22 sixty and 5.22@136 on a relatively mild tune.
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We got back Sunday morning and the track was definitely more crowded. We made one hit early that went well but the car slowed down a little with the shock adjustment we tried and as the day progressed it just got worse. That first pass ended up being the ONLY pass we made that day that the car didn't blow the tires off. Saturday we made 4-5 passes and never spun. WTF

On the one pass we did make on Sunday we found the crankcase pressures got really high and suspected the vacuum pump was backing up. So we disconnected it and just vented the crankcase which fixed the issue. I had been messing with that vacuum pump for awhile and thought I could get it to work but it just can not keep up. Possibly a larger vacuum pump will work which I may try but with no pump I had zero crankcase pressure which was good to see. It reached 9psi with the vacuum pump and was pulling close to a quart of oil out.

We did get the car tech in on Sunday which was nice to be able to get that done early as it usually takes most of the day to get done on Tech Day.
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Tech Day was a total washout, it never stopped raining the entire day. I was at the end of the life cycle for my tires and had a new set put on my Mickey Thompson at the track which worked out well. We put all the suspension settings back to what we ran on Saturday and neutered the starting line tune up and waited for Day 1.

Race Day #1. The morning was cold and wet and the track was still soaked. They didn't get the day started until almost 11:30 and decided to put the slower C&D groups down the track first with the AB Radial group going next to last. We are usually the first. We didn't get called to the lanes until almost 3pm.
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When I rolled up to the line Ray said the track was a mess and had strings of glue coming off my brand new tires. I did a good burnout to clean up the new tires, staged and the car spun as soon as I let go of the button. I pedaled it some and stayed in it for a 10.32 pass and was bummed it was not going to be a one and done day and we now had to wait for the all run session. This really sucked because the drive to Bradenton was the longest one at 320+ miles and it was already close to 4pm when we completed that pass. Day light was fading and they still had a shit ton of cars in the lanes. So we waited.
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I backed the starting line tune up down to softer than when we started testing but it didn't matter, They ended up calling the day around 5:30 and were finishing out the lanes so everyone got one run for the day and I had to turn in a 10.32 slip while the top guy in the class Cooper Bogetti managed a clean 8.52. That is going to screw us for the week bad but were weren't the only ones and I still mathematically had a shot since Cooper was not legal to run under 8.50. I needed to turn up my game though and unfortunately we didnt not get enough testing with the new combo to know exactly what the car was capable of. We loaded up and got on the road around 6:30 in the dark. The drive to Bradenton was pretty unremarkable. On tech day I did get the Gearvendor hooked up and working and we tested it with the Holley controlling it and it worked fantastic. Being able to blast down I75 at 75mph and 2600rpm really saved us a shit ton of time and an exhaustingly long trip. With the one check point it still took over 7 hours and we didn't get into the hotel room until alomst 2am.

The one checkpoint was pretty cool a new race track, we didn't hang out long though
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We were back up at 5:30 am and at the track by 7am with a refreshing 3 hours of sleep. We got the car swapped over, on the way down we ended up running pump gas in the car and noticed the car ran really rich with the ethanol content down around 20%. We ended up putting E85 back in which brought it back up over 50% cleaned it up a lot and the car really ran a lot better. We drained the gas and were running a leaded race blend E85 from Renegade on the track.

Bradenton had a good track prep, I know SGMP is also known for being a good track with the the weather struggles they had it was difficult. Not so much in Bradenton it was actually pretty warm that day. They called AB radial as the second class that day. I staged bumped in and had to hit the bump a second time and the car just launched. I think since the track was so sticky it jerked the car some and my thumb must of come off the t-brake enough to release it. The log showed it engaged twice but IDK, it sucked as I did not set the tree or get a time slip, so once again we had to wait for all run. The car did hook and I made a full pass but the car was really lazy and seemed to really slow down. Ended up we forgot to remove the air filter on the new inlet Ray built!!
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To this point we are like WTF, Drag week was almost to easy and Sick Week has been a shit show up to this point. We have a car that should be in quarantine and on top of the class and we can't even get down the track. It is now Tuesday and we haven't made a clean pass on the car since Saturday!

Finally we got a hit on the car with a very mild tune up. The car felt good but was still off a little bit from where it should have been but it was a nice A to B easy peasy 8.32 pass. We handed in the slip and got on the road. The math was easy a 10.32 and a 8.32 now gave us a 9.32 avg and moved us from 18/23 to 4th. Not bad, to date I also believe it was the fastest pass in the Street Freaks class. If we leave the car like this we have a real shot, but we also know the car has a shit ton more left it in for later in the week.
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Loaded up and on our way. We put the 50% ethanol gas we had in the tank back in and got on the road. We needed to fill up when we left and only had a few options for an E85 station which were all out of the way. We stopped and decided to just run pump gas again. The car ran fine but it did not want to idle well and surged a bunch. The Billet Atomizer injectors really like the ethanol a whole lot better and seemed to struggle with the low pulse width needed for pump gas.
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We made the first check point fueled up and started our trek across the state to the other side through the forest preserve and swamps of central Florida. There was nothing along this road and at night it was pitch black with no lights other than headlights of cars and trucks blasting down the two lane road. Fortunately the majority of traffic was Sick Week'ers at some time around 8pm or so the car decided to just die on the side of the road. We pulled over into the gas/weeds to get off the road and saw smoke and smelt gas really bad. We looked it over and were not able to find anything visibly wrong. We tried cranking the motor and it abruptly stopped cranking which wasn't good. Ray was literally getting eaten alive by what ever creatures lived in that grass, it was pitch black and we had semis and traffic blasting by use at 70 mph. Not a good scene and very dangerous.

Fortunately we had a bunch of racers stop to help. We decided we need to get the car off the road to a safer location adn there was a driveway or road right up a little ways. I did not have the tow hook on the car and I did pack it but for some reason we could not find it. After some quality engineering we cut the safety chain off the trailer and was able to fit it in the hole for the tow hook put a bolt through it and make a make shift tow strap which we tied to the the rear bumper support of a 1957 Chevy station wagon gasser! These guys saved our asses and ended up towing up at least 5 miles to the Racetracs gas station.
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The name on thier car was Lucky Draw as they won the car in an online raffle by Mike Finnegan. We actually ran into these guys earlier at a taco stand the story about winning the car last month blowing up the motor and then doing Sick Week with it was incredible. These guys were definitely having a blast doing this.

Us not so much lol! We still weren't out of the race since you are allowed to be towed to safety. This Racetrac was at the end of this 40-50 mile stretch adn literally everyone stopped at it. When we got towed in the place was packed with racers. We got to work on the car and found that injectors had locked up and hydrolocked the motor. We ended up getting it to pump the gas out but when we went to try and start it again it did the same thing. After messing with it and getting a lot of expert help from Brandon Doller we finally called it a day around midnight. We thought the motor lost a timing chain at first and called our buddy to come get us with his truck and trailer. We were close to I95 on the east coast down near Melbourne close to 400 miles away from the truck and trailer. Literally the furthest distanxe you can possibly be on the route. We worked on the car until Murray showed up at a little after midnight. We towed 2.5 hours to his place and got a few hours sleep got up and continued on to Georgia. We loaded up and then headed home getting in at 8am Friday running on a total of 7hours of sleep since Tuesday.

I am still taking it all in, even as prepared as we were we still didnt do well and we brought a car that should have dominated our class. But we were again untested, we never ran pump gas in the car before and we had a new cam combo that added a lot of power down low and made the front half of the track a little more difficult. Both of these things stung on on this event.

The good news is after getting the car home, I took the injectors apart and cleaned them drained the pump gas and put the race tune and race E85 back in the car and it fired right up like nothing ever happened. It is what it is had we known the exact problem then we would have been able to continue but we didn't. Plus we were running into goofy battery and starter issues at the same time that ended up being simple problems too. As for now, I am going to focus on getting this car finally sorted out. Sick Week is really difficult when you are coming from Ohio in January. Winter makes everthing 100x more difficult and we experienced that 2 years in a row now. Plus the days are really short even in Florida which means almost all your driving is done at night and the tracks shut down early. I am not sure I will go back next year but we will see. I am signed up for Sick at the Rock in April where I hope to get some good track time on the car and finally get it in the 7s.
 
Sounds like you had a big week. Those drag and drive's are pretty brutal. Thanks for the details!
 
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