So I get my T-type out today and Since I have no access to 110 Race fuel I ordered a new chip and change it over to 93 octane and Razor Dual Nozzle Alky system.
When I put it away last year it was 100% fine. New chip should not change any thing on the boost side.
Took it for a ride to get my son from school and Punched it out of the gas station boost went over the 35PSI my gauge shows and I let off It knocked of before I saw the gauge. So I twist the Dial down on my Manual boost controller in the center console Hit it again same thing no change. Dialed it all the way down hit it again Same thing.
At this point Im pissed because I have to get my son and I just drove it nice and got him. he says get on it daddy I CANT! He gets mad.
So I get home I pull the lines off the External gate and expect to find a hole in one. No holes! I hook the Air compressor up and put some air to them with Manual Controller off. Does as it should no air out the one side. Dial it up somewhat it should do small amount out the other side. (Also should not I blocked off the connection at the turbo for these little tests) Next I opened it up and as it should same about in as out. All good there.
Tested off the turbo line to the gate all fine.
So what else do I look for the simple is obviously not it. Should I open the gate up and check inside? Anyone ever have this issue before?
I was told the wastegate is an old ATR external Gate. I cant find any parts for the thing online. Im Thinking the Diaphram in it has cracked maybe? Spring is a 10psi in it so even with the gate shut it should only be that much. I cant dial this mess down its over 35PSI NOT GOOD
Any help advice would be great
thanks for reading and helping
When I put it away last year it was 100% fine. New chip should not change any thing on the boost side.
Took it for a ride to get my son from school and Punched it out of the gas station boost went over the 35PSI my gauge shows and I let off It knocked of before I saw the gauge. So I twist the Dial down on my Manual boost controller in the center console Hit it again same thing no change. Dialed it all the way down hit it again Same thing.
At this point Im pissed because I have to get my son and I just drove it nice and got him. he says get on it daddy I CANT! He gets mad.
So I get home I pull the lines off the External gate and expect to find a hole in one. No holes! I hook the Air compressor up and put some air to them with Manual Controller off. Does as it should no air out the one side. Dial it up somewhat it should do small amount out the other side. (Also should not I blocked off the connection at the turbo for these little tests) Next I opened it up and as it should same about in as out. All good there.
Tested off the turbo line to the gate all fine.
So what else do I look for the simple is obviously not it. Should I open the gate up and check inside? Anyone ever have this issue before?
I was told the wastegate is an old ATR external Gate. I cant find any parts for the thing online. Im Thinking the Diaphram in it has cracked maybe? Spring is a 10psi in it so even with the gate shut it should only be that much. I cant dial this mess down its over 35PSI NOT GOOD

Any help advice would be great

thanks for reading and helping