novaderrik
Well-Known Member
- Joined
- May 12, 2004
- Messages
- 8,076
eliminated.. or at least minimized.
i got rid of a little bit of a restriction in my stock up pipe today. it had actually blown out a few years ago, but i "fixed" it by wrapping a band clamp around it to get by. well, the clamp wouldn't seal any more so i took it apart.
this is what the pipe necks down to in the flex coupler in the middle of the pipe:
granted, the rest of the pipe is only a little over 2" inside diameter, but that 1/4" reduction in diameter was worth about .55 square inches of cross sectional area, which is about a 20% reduction if my math is right. feel free to correct me on that, tho.
i cut out the stock coupler and welded a piece of 2.125 i.d. exhaust pipe in it's place. i haven't driven it yet, but between getting rid of the leak and increasing the flow, it should run a little better. not a 12 second terror yet, but probably better than it was. i know it feels snappier in park at idle and is quieter without the constant 'pfft pfft pfft'..
tomorrow, i'm gonna wrap the pipe to make it look better (welded with flux core wire...) and keep more heat in it.
someday, i'll get some mandrel bends and make a better pipe without the craptastic factory bends. but for now, this will work.
here's what it looks like right now. click on the pic for a closer view:
i got rid of a little bit of a restriction in my stock up pipe today. it had actually blown out a few years ago, but i "fixed" it by wrapping a band clamp around it to get by. well, the clamp wouldn't seal any more so i took it apart.
this is what the pipe necks down to in the flex coupler in the middle of the pipe:
granted, the rest of the pipe is only a little over 2" inside diameter, but that 1/4" reduction in diameter was worth about .55 square inches of cross sectional area, which is about a 20% reduction if my math is right. feel free to correct me on that, tho.
i cut out the stock coupler and welded a piece of 2.125 i.d. exhaust pipe in it's place. i haven't driven it yet, but between getting rid of the leak and increasing the flow, it should run a little better. not a 12 second terror yet, but probably better than it was. i know it feels snappier in park at idle and is quieter without the constant 'pfft pfft pfft'..
tomorrow, i'm gonna wrap the pipe to make it look better (welded with flux core wire...) and keep more heat in it.
someday, i'll get some mandrel bends and make a better pipe without the craptastic factory bends. but for now, this will work.
here's what it looks like right now. click on the pic for a closer view: