BLM at idle wasn't too bad at 134.
I'm ignoring my WB until I have moved it further away from the turbine housing. I have the chip in its base settings, with the alky turned off. I'm not going to touch timing or boost until this is fixed.
I didn't check the 1:1 rise on the mechanical gauge. It looks like my autometer gauge reads 10psi low.
I did a leakdown check on the system while I had the gauge hooked up. It held pressure fine. I was going to do an injector balance test, but I couldn't find my injector tester.
I will find the cause of the problem. It's just going to take a while...and it's going to be something small, and stupid. (high resistance in a connector, a crappy, unrelated ground..) I refuse to throw parts at the problem.