BennyBuick
Member
- Joined
- Sep 10, 2014
- Messages
- 67
Decided to listen to the advice here, we will reassemble without header gaskets and use the high temp copper stuff. The header gaskets were completely shot with full layers missing. The waste gate was fine, the issue was the gasket between turbo and down pipe/waste gate. It was completely blown out around the wastegate hole and I'm sure that was what caused me to lose boost instantly. The moment that gasket finally let go and blew out, boost no mo. My mechanic will also do a vacuum leak test as well for good measure. I'm wondering how this thing is going to run on the test drive after reassembly, the temp will probably be in the 20s or so here in central il.